@techreport{oai:jaxa.repo.nii.ac.jp:00043984, author = {渡辺, 実 and 鳥崎, 忠雄 and 武田, 克己 and 小林, 紘 and 関根, 静雄 and 中山, 普 and 吉田, 晃 and 越沼, 威 and 松田, 幸雄 and WATANABE, Minoru and TORISAKI, Tadao and TAKEDA, Katsumi and KOBAYASHI, Hiroshi and SEKINE, Shizuo and NAKAYAMA, SUSUMU and YOSHIDA, Akira and KOSHINUMA, Takeshi and MATSUDA, Yukio}, month = {Jan}, note = {Inlet and fan exhaust noise suppressors for a high by-pass ratio turbofan engine (FJR710) were ground tested.The inlet and fan exhaust duct walls were lined with perforated-plate-on-honeycomb absorbers.Acoustically treated splitter rings could be inserted into the inlet duct for a greater noise attenuation.The inner and outer walls of the annular fan exhaust duct were lined with different depth absorbers for a broader band noise attenuation.Sound power attenuation spectra were obtained by an insertion loss technique using far field measurements.Noise from each treated duct was compared with noise from a hard wall duct without splitters.A maximum perceived noise level attenuation due to the suppressors of 16 PNdB was obtained at 95% fan speed.Degradations of engine performance caused by the fully equipped suppressors with splitter rings were about 3% of the engine thrust.No detectable thrust loss was measured in other experimental cases without splitter rings., 資料番号: NALTM0401000, レポート番号: NAL TM-401}, title = {ファンエンジンFJR710による吸入消音ダクト及びファン排気消音ダクトの地上実機試験}, year = {1980} }