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  2. 紀要論文 (Departmental Bulletin Paper)
  1. 機関資料(JAXA, former ISAS, NAL, NASDA)
  2. 旧機関資料 (JAXA, former-ISAS, NAL, NASDA)
  3. 宇宙科学研究所: ISAS Report等を含む (former ISAS (The Institute of Space and Astronautical Science): Including ISAS Report etc.)
  4. The Institute of Space and Astronautical Science report

On the Simulation Test for the Relative Motion of Separated Sub-Boosters on M-3SII with Nearly Half a Model Vehicle ST-735 and their Motion Analyses Using Inertial Sensors Output

https://jaxa.repo.nii.ac.jp/records/31401
https://jaxa.repo.nii.ac.jp/records/31401
f00eb5a6-c4c7-4588-95a6-034fcc3f2777
名前 / ファイル ライセンス アクション
SA0035086.pdf SA0035086.pdf (951.7 kB)
Item type 紀要論文 / Departmental Bulletin Paper(1)
公開日 2015-03-26
タイトル
タイトル On the Simulation Test for the Relative Motion of Separated Sub-Boosters on M-3SII with Nearly Half a Model Vehicle ST-735 and their Motion Analyses Using Inertial Sensors Output
言語 en
言語
言語 eng
資源タイプ
資源タイプ識別子 http://purl.org/coar/resource_type/c_6501
資源タイプ departmental bulletin paper
著者 TSUKAMOTO, Shigeki

× TSUKAMOTO, Shigeki

en TSUKAMOTO, Shigeki

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出版者
出版者 宇宙科学研究所
出版者(英)
出版者 Institute of Space and Astronautical Science
書誌情報 en : The Institute of Space and Astronautical Science report

巻 635, p. 1-15, 発行日 1989-02
抄録(英)
内容記述タイプ Other
内容記述 In the course of development for M-3SII type vehicle which has two relatively large sub-boosters, a possibility of collision between the separated sub-booster and the core-motor was discussed with concern especially in relation to the effect of the core-motor plume. We had a flight simulation test under the conditions specified by the similarity law given in this paper with ST-735,nearly half a scale model of M-3SII, and the relative motion of the sub-booster was analyzed with on board TV, inertial sensors and a measuring device of separation distance. Althouhg TV pictures provide us with real time, high speed images of the sub-booster, only 2 dimensional information is obtained in principle. Analysis on the motion with 12 inertial sensors informs us of a complete 3 dimensional motion of the sub-booster. We could predict from the test that the exhaust plume would not influence on the motion of the separated sub-boosters in M-3SII flight.
ISSN
収録物識別子タイプ ISSN
収録物識別子 0285-6808
書誌レコードID
収録物識別子タイプ NCID
収録物識別子 AA10632072
資料番号
内容記述タイプ Other
内容記述 資料番号: SA0035086000
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